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以模拟生活污水为处理对象,重点研究了在硝化液回流比(α)为100%,内循环回流比(R)分别为100%、150%、200%条件下A3/O-MBR工艺脱氮除磷特性.结果表明,内循环回流比对COD、NH4+-N和TN去除影响较小,COD、NH4+-N和TN平均出水分别小于50、2和20 mg/L,去除率分别保持在95%、97%和70%以上.TP去除率随回流比增大而增大,在进水平均TP质量浓度为4.26、7.68和7.70 mg/L条件下,平均TP出水质量浓度分别为1.67、1.31、0.99 mg/L,去除率分别为60.80%、82.94%和87.14%.同时增大内循环回流比有利于厌氧区磷的释放及缺氧Ⅱ区磷的吸收,释磷量由0.252 g/d增加至1.864 g/d,吸磷量由0.108 g/d增加至2.160 g/d.“,”Using the synthetic domestic sewage as treatment object,focused on the A3/O-MBR process characteristics ofdenitrification and phosphorus removal when nitrate recycling ratio (α) of 100%,and internal return ratio (R) as 100%,150%,200% respectively.The results showed that the removal rates of COD,NH4+-N and TN are almost not influenced by the change of internal recycle ratio,and the effluent concentrations of COD,NH4+-N and TN less than 50,2,20 mg/L respectively.As while as the average removal efflciencies more than 95%,97% and 70%,respectively.However,the removal efflciencies of TP increased with the increasing of the internal recycle ratio.The average influent concentration of TP was 4.26,7.68 and 7.70 mg/L and the effluent concentration of TP was 1.67,1.31,0.99 mg/L respectively.The removal efficiencies of TP were 60.80%,82.94% and 87.14%,respectively.Meanwhile the release and uptake of phosphorus in the anaerobic zone and anoxic zone Ⅱ was increased with the increasing of internal recycle ratio,and the release rate increased from 0.252 g/d to 1.864 g/d,the uptake rate increased from 0.108 g/d to 2.160 g/d.