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为降低挂面生产的劳动强度,改善劳动条件,提高生产效率,目前挂面厂大都实现了连续性机械化作业。但目前的挂面自动下架设备不够理想。我省有不少单位出现因面筷在烘道内运行歪斜而导致下架落杆多的现象,影响了产量.有不少单位的下架设备或因达不到理想效果而不用,或需派专人看管. 今年,我厂在生产实践中,经过多次摸索、分析,试制了重力式自动下架控制器.其原理为控制器通过其调节压块,给予面杆一定阻力(其阻力可根据一杆面的重量进行调节),
In order to reduce the labor intensity of noodle production, improve working conditions and improve production efficiency, most of the current noodle factories have realized the continuous mechanization operation. However, the current noodles automatically off the shelf equipment is not ideal. There are many units in our province due to the chopsticks in the drying tunnel run skew and led to the phenomenon of falling bar under the rack, affecting the yield. There are a lot of units of equipment or due to reach the desired effect is not, or need to send This year, I plant in practice, after repeated exploration, analysis, trial production of the gravity-based automatic rack controller. The principle of the controller through its regulation of the block, to give a certain resistance rod (the resistance can be based on A face weight adjustment),